Welcome to the Meany Work Party Page
If you have been wondering what it takes to keep Meany going, come to one of the Workparties held in
the Summer and Fall and see what it takes. Workparties are free and offer a great opportunity to
enjoy the lodge in a different light. You can learn new skills or brush up on old ones that your
'real' job doesn't let you do anymore. There is also time to get to know folks over work and
conversation.
We offer mid-week and weekend workparties, If you want to attend any of these simply click on
work parties, pick the weekend and sign up.
Work Party Reports
Please click on any of the months below to go directly to that section or simply scroll down
June Mid-Week Report
The June mid-week WP was held Tuesday June 28th through Thursday June 30th. The
weather was cool with some sun and a bit moist from time to time.
The following were there:
- Phil Christy
- Dave Claar
- Doug Damm
- Don Finrow
- Bob Grass
- Linda Harkness
- Lee Helser
- James Kotlik
- Mike Lonergan
- Emilio Marasco
- Julianne Marasco
- Dan Solomonson
- Ray Nelson
- Patti Polinsky
- Tom VanDevanter
- Norm Vigus
Note: It was good to see the younger set joining us. It improved the WP.
Webmaster note:
And it was a girl no less!
The following was accomplished on this WP and items noted for decision.
- Ox was freed and put into use. It was used to lift off the head pole and safety gate poles
for the Snail Tow (Turtle Tow). After the work it was noticed that the right front tire ws split rim
to rim. The wheel was taken to town and the replacement tire mounted. It will be installed next WP.
- Snail Tow (Turtle Tow) new head pole and two safety gate poles were delivered and the old ones
taken down in preparation for back-hoe work at next mid-week WP. We expect to dig the three holes for
the poles (with a track hoe) and place the form work, anchor bolts and rebar. The concrete will be
poured on the August WP and the poles erected on a future WP.
- The back-hoe will also be used to repair the access road (FR 420) up from the creek and any other
work that comes to light, time available.
- Several loads were taken to the dump. The Lodge, Phone Cabin and surround areas is now fairly
free of garbage.
- The gate at Railroad curve was repaired.
- The Phone Cabin was cleaned up, painted and readied for use for the Women's weekend.
- Several water leaks in the kitchen:
- Faucet for the pot cleaning sink failed and was replaced
- Valve in the dish washing sink was replaced
- Strainer basket was reinstalled and does not now leak
- Valve for the sink next to the stove was repaired
- Valve for dish rinsing brush was not repaired, no parts on hand, will be repaired next WP
- Tow report
- General note: Electric tows VFD's were turned off. Should be left on to preserve electronics
- Mach tow
- New carberator needs (see comments under TomCat issue)
- Braking system was inspected.
- The actuator arm was adjusted.
- Differential oil needs changing along with the regular tow servicing
- Support cable for the tail wheel needs tightening
- Ground wire needs to be reconnected to the transformer at the back of the tow hut
- More work will be done during next WP
- Super Worm (Worm) tow - There is considerable slack on the top rope of the safety gates that should be
corrected.
- Snail (Turtle) tow - Slack in the safety gate rope but is now removed to be reinstalled
later with the installation of the new poles
- TomCat - Returned to the lodge, the following was noted:
- Carburetor is nearing its life expectancy - Recommended replacing with two barrel carburetors
- Roof support bracing has broken and/or bent and thus is in need of attention
- Throttle cable needs to be replaced - recommend purchasing of two new throttle linkages
- Exhaust system - recomment new flexible exhaust connectors and donuts for the exhaust system
- 2nd tow rope replacement - material located on the second floor of the Cat House
Please note: Work by the fossils on the the above tasks will likely be
limited this year due to other projects (see below Moose) and available time. The "young" crew will
need to pick up the slack here
- Moose was inspected and we found:
- More extensive damage in the areas of the cracks found earlier. Welding will occur during next
WP.
- Need to remove hydraulic lines to the drive motor so as to be able to weld damaged areas.
- Need some hydraulic port covers for the motor so as to be able to weld on the frame.
- Left side axel, just ahead of the drive sprocket, was found to be broken and was removed.
Brought back to town for a sample to get a replacement part. Note that is is appearing that there
may be some difficulty in getting this part.
- Controls were found to be at the end of its service life and were removed. Will need to replace
control console
- hydraulic leak on the floor of the Zoo. Unable to clean it up due to the lack of kitty litter. We
will correct this problem at the next WP.
- 6 or 7 bad wheel guides and we have only two on hand. We are going to get the necessary wheel
guides and a couple of spares.
- Grousers were not checked as we did not have them turned over. Needs to be done sometime this
year
.
- Pac Rat was looked at very briefly and was discussed some. No work can be preformed until
a decision is made about its future:
- Fix it up and use it. Not recommended, it is weak and parts are getting harder to get
- Fix it up and sell it. Not recommended, this will take time that we do not have much of
- Sell it as is along with miscellaneous parts and sell major parts (ie differential) separately -
Recommended option
- If we choose to replace, it should be a cat similar to the Pac Rat that is a newer model with
either a deck or passenger cabin
- The basement was cleaned up for the upcoming events at the Lodge
- Several damaged and/or dying trees were cut down and cut up for fire wood
- A path was cleared for the two large dead trees behind the Tow Hut and we expect to take them
down on the next WP
- Work was began on replacing the fire escape from the fourth peoples dorm (new anchor attachments
were installed). It was left in place temporarily for the upcoming events at the Lodge. It is
expected that it will be replaced at our next WP
- Smoke detectors in the Lodge were inspected and found to be working. There are two missing and
a third damaged. We will get the replacements and batteries for the next WP
- All generators were test started and loaded. All worked as they should
- Repairs were made to the hand rail for the stairs to the generator hut
- An insulator on the neutral off the power line is off near the Lodge and will be repaired later.
July Mid-Week Report
The July mid-week Work Party was held Tuesday July 12th through Thursday July 14th.
The weather cool with some sun and a bit moist from time to time.
The following were there:
- Phil Christy
- Dave Claar
- Doug Damm
- Bob Grass
- Lee Helser
- Mike Lonergan
- Ray Nelson
- Patti Polinsky
- Phyllis Nelson
- Tom VanDevanter
The following was accomplished on this WP and items noted for decision.
- Ox runs (the wheel with the new tire has been placed on the Ox), however it is likely that
it will need of a new fuel pump and/or fuel filter.
- tracked back hoe was delivered and the 420 road was graded to some extent. Some drainage
work was done and the water bars were cleaned out by hand. Also some handwork was done to keep the
creek in the channel near the 54 road.
- Turtle Tow head and safetey gate pole holes were dug. Work was done on transferring
the wheel assemblies to the new head pole.
The placement of the rebar, mounting bolts and framing will be done at the next work party. The
placement of the concrete (approx. 26 yards) will be done on a special purpose work party sometime
after the regular midweek work party.

Bob Grass at the helm digging holes

Mike Lonergan adding finishing
touches

And the reason for all the work, Turtle's fancy new head pole

Dave Clarr and Phill Christy spreading the dirt over the culvert across the
Junior Trail
- Grass and weeds were mowed in the area of the Tow Hut.
- Mach Tow brake air line was replaced and the tow stopping distance retested. It was
found to stop in a shorter distance than previously. Obviously, when the new rope is put on, it will
again need to be tested for stopping distance. Note, the rope was hung in preparation for concrete
delivery.
- Moose frame welding repair work was done. More welding to be done in other areas which
will involve removing several hydraulic lines from the drive motor.

Red circle shows the weld repair with re-enforcing plates.
Green circle shows hydralic lines to be remove to perform
further welding
As a further note on the Moose, we now have new controls in our possession and will be installed at
the next work party. The wheel guides and broken grousers may get replaced then.
Zoo hydraulic oil spill under Moose was cleaned up in preparation for continuing repairs.

Phyllis Nelson cleaning up under Moose
Webmaster Note: See, the Meany women always have to clean up the
mess the Meany men make
Repairs using this method could wind up expensive.
The following was accomplished on this WP
A considerable amount of brush and limbs were burned up. Most came from an earlier tree
trimming exercise for the power line.
- Cat House lighting was rewired and a switch located on the outside.
- Moose, several minor items were completed, tracks installed and Moose driven.
NOTE: We noticed an hydraulic oil leak from the bottom or back of the storage
tank. You will likely have to live with this for the winter season and watch the oil level and fill
when necessary
Leak on blue tower, starting on day one
Leak after 24 hours
Moose on the move
- New two barrel carburetor was installed on the Mach Tow. On test run it seemed to perform
considerably better
NOTE: The air cleaner adapter needs 4 bolts to connect it to the carburetor
(3-5/16" x 4" NF & 1 5/16" x 4.5" NF). We did not have them
New carburetor and air cleaner adapter
- Turtle Wiring - Wiring at the bottom of the steel safety gate pole was completed. The actual gate
is left for others to complete.
Turtle Wiring
Giving Tom Dunstan the credit!!!
- Fuel was delivered. We got 250 gallons of diesel and 670 gallons gas. There was a problem
where approximately 100 gallons of diesel was put in the gas tank near the Lodge. This was pumped back out
but we did not get it all because of a failing gas pump. The fuel was later tested (the next weekend) and
found to be ok and not in need of being replaced again. To prevent this problem from reoccurring, the gas
house and tanks should be marked Gasoline. The diesel house is marked. Further, others found the filter
and screen to be plugged. I understand that the screen was cleaned (on the pump itself) and an in line
filter removed. This filter should likely be replaced.
- Two truckloads of gravel were placed on the 420 road.
- 1940 pounds of scrap steel was taken to the recycler.
- Sign board near Turtle needs to be set back up. A post hole digger would be most helpful for
this task.
- Mach Tow needs new spark plugs. Oil and filter needs to be changed.
- Hard Rain We had days of heavy raing. Water bars on the roads handled the runoff well
Trolley Replacement Report
Trolley Removal
As some of you may have heard, the Mach head pole trolley had a catastrophe failure during the winter. And
thanks to the quick thinking of Jimmy and Nigel, a work around (ie heavy duty cargo strap) was used that got
us through the rest of the season. But a new trolley was definitely needed, so during a weekend in July, a
group led by Jim Fahey and Nigel Steere went to the top of the lane to remove it.
It started with Jimmy driving his Suburu across the lane, to the quarter tower in order to unhook the
rope. Interesting feeling, crossing the lane with the driver side lower then the passenger side. The next
step was to drive down (yep down the lane) to the Tow Hut. Once there, we proceeded to to lower the
counter-weight to take mach out of tension. After that, our curiosity got the better of us, so the last
image is of the new Turtle Tow Towers

Jimmy at Quarter Tower

Dropping counter-weight

Turtle Towers
The next step was to get to Mach's head pole. You would think we would need to hike up the lane. Nope
Jimmy had it all figured. "Why don't we take the scenic route to the top". And of course with
signs like the oned below, how can one ever get lost. Thank goodness Jimmy knew the way. So, once we
were at the top of south (the real top), Jimmy turns down the road that lead to the head pole. Yep
another 45° incline (or close to it) and parks near the ramp.

Very descriptive road signs

Jimmy, you are not serious ?

We made it !!!
Once at the top, the fun now began, here is a series of images of Nigel and Jimmy scampering around
the head pole and finally lowering the trolley, along with image of pulley axle and nut

Nigel

Jimmy

Trolley being lowered
The next series of images show the damage done to the trolley and why Nigel thinks it needs to be
refrabricated

Trolley Damage

Trolley Damage

Trolley break
So with the trolley stached in Jimmy's Sabaru, it was time to go home. So, Jimmy decides that to get
back up, he needed more traction/weight on the wheels, and the best way to do accomplish that is to
drive backwards up the incline he came down on!. the first image is of the tires slipping,
(both Nigel and I were wondering if this was a sign that we wouldn't get home anytime soon). The next
one (of course) is of Jimmy at the top looking very proud of his accomplishment. (Next time you see
him ask him about his adventure with his mini-cooper). Final picture of the view from the real top of
South.

Subaru Slipping

Pround Jimmy

Top of South view
Trolley Installation
During the month of September The new trolley was installed. It took two trips. The First one, with the
help of the support crew (Hudson, Juliana and Milo), Nigel got the trolley installed. Fine tuning was
done the second September trip. The end result was a brand new trolley with a cable and winch for
height adjustment, along with a new climbing rope as a static backup to the winch system.

Trolley

Winch
Mach Safety Ramp Upgrade
During the 2010-11 winter season, it became apparent that Mach Tow’s safety ramp needed some TLC. During the
spring committee meeting it was decided that we should replace the ramp’s surface. Thanks do Nigel Steere's
bother-in-law, we had a 4X4 truck and were able to deliver the intial load of 2 X 4 during the Trolley
installation work party early in September. At that time the old The 2 X 4 ramp surface was removed by yours
truly. During said removal, it was determined that the log support structure was severely rotted and would
need to be replaced. Since new logs were needed, Phillip went out choose and cut three approprate trees. With
the help of all who attended the Wilderness First Aid class, the logs were moved to the top of the lane on the
September 22nd work party. These new logs would allow us to extend the ramp about 5 feet, from 22’
to 27’ in length. The extra lumber, needed for the expanded ramp surface, along with the supporting struture
once again was delivered by Nigel and his brother-in-law's truck.
The ramp upgrade crew consisting of Brian Finrow, Christopher Springer, Dan Nord, George Howard, Mark Abrams
and Phillip Christy, started working on the October 6th work party and completed the project at the
October 22nd, 2011 work party. The following set of pictures begin with the placing of the support
logs

Determining that we could not lift logs by bruth force alone

Setting up mechanical assist

Using it to Lift second log
Once logs were placed, new ramp surface was screed to the logs. As it progressed extra support timbers were
tied into the ramp logs to carry to upper weight of the ramp

2 X 4 lumber being use to create
ramp surface

View of extra supporting structure
needed

finishing ramp
So here it is finally in all its glory --- and no Nigel, you can't use it as a snowboard
ramp

View up the ramp

View of the extra support needed for extension